Title of article :
Study of the catalyst deactivation in an industrial gasoil HDS reactor using a mini-scale laboratory reactor
Author/Authors :
Kallinikos، نويسنده , , L.E. and Bellos، نويسنده , , G.D. and Papayannakos، نويسنده , , N.G.، نويسنده ,
Issue Information :
روزنامه با شماره پیاپی سال 2008
Pages :
6
From page :
2444
To page :
2449
Abstract :
The activity of a hydrodesulphurization catalyst loaded in an industrial hydrotreater is studied at start up and end of run. Catalyst initial and final activity was determined by performing HDS experiments at industrial conditions in a laboratory mini-scale hydrotreater. The results show that the deactivation of the catalyst samples collected from three different places of the industrial reactor do not vary significantly, the maximum difference among the catalyst samples, being less than ±4%. The experimentally determined deactivation level of the catalyst samples is compared with the deactivation estimated for the same industrial reactor and the same load using a hybrid neural network model trained with operational data of the industrial and the results are in close agreement. Catalyst deactivation appears to be faster for hydrogen consumption reactions than for hydrodesulphurization reactions indicating a decreasing hydrogen consumption trend with time in operation for specific sulphur content in the product.
Keywords :
Mini-scale reactors , Multiphase systems , Reactor model , HDS reactions , Catalyst deactivation
Journal title :
Fuel
Serial Year :
2008
Journal title :
Fuel
Record number :
1464587
Link To Document :
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