Title of article :
Fatigue failure of an aircraft wings due to fitting error in hi-locks
Author/Authors :
Mansoor، نويسنده , , M. and Ejaz، نويسنده , , N.، نويسنده ,
Issue Information :
روزنامه با شماره پیاپی سال 2009
Pages :
7
From page :
2195
To page :
2201
Abstract :
Two hi-locks were fractured during a flight of a carrier aircraft, causing the leakage of fuel in the right wing section. The failed and a new hi-lock were subjected to failure investigation. al of the hi-locks was AMS-6270. The hardness of both hi-locks was also comparable to each other. The investigations entailed that the failed hi-locks were loosened or improperly preloaded. Thence the fastened sections exerted bending fatigue loads on the hi-locks. Therefore, two propagating beach mark fields were observed on the fracture surface, which were advancing towards each other under high cycle fatigue (HCF). When the crack reached at the threshold level, the hi-lock(s) failed catastrophically.
Keywords :
Improper preloading , Fatigue , Hi-lock , High cycle fatigue , AMS-6270
Journal title :
Engineering Failure Analysis
Serial Year :
2009
Journal title :
Engineering Failure Analysis
Record number :
2338685
Link To Document :
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