Title of article :
Failure analysis of heat exchanger fluid vapor phase vent lines in a Polyester plant
Author/Authors :
Virk، نويسنده , , M.A. and Butt، نويسنده , , M.A. and Chughtai، نويسنده , , A. and Ahmad، نويسنده , , M. and Khan، نويسنده , , I.H. and Deen، نويسنده , , K.M.، نويسنده ,
Issue Information :
روزنامه با شماره پیاپی سال 2010
Pages :
8
From page :
447
To page :
454
Abstract :
A Polyester plant is using Proprietary heat exchange fluids (26.5% biphenyl, 73.5% diphenyloxide). The plant hot condensate tank, condensate feed tank, and heat exchanger vapor phase dead end and ventable lines (ASTM 106 Grade B) with isolation valves were suffering frequent leakages with severe gouging and pitting corrosion. Lustrous (shiny) coke deposit was prominent inside the cut sections due to coke formation by low boiler products. Some adhered brown iron oxide (rust) deposits were also visible. A sludge sample was analyzed by XRD which revealed that carbon was the major constituent with γ-Maghemite-C (an iron oxide) as second mineral in order of abundance. The failure was diagnosed as severe localized corrosion and gouging at temperatures of about 200 °C and 53 psi by non-condensable low boilers decomposed corrosive products. The remedy was suggested which has been validated over the 2 years trouble free performance.
Keywords :
Gouging , Pitting corrosion , Failure , iron oxide
Journal title :
Engineering Failure Analysis
Serial Year :
2010
Journal title :
Engineering Failure Analysis
Record number :
2338879
Link To Document :
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