• Title of article

    Failure analysis of an aero-engine combustor liner

  • Author/Authors

    Lv، نويسنده , , Fengjun and Li، نويسنده , , Quan and Fu، نويسنده , , Guoru، نويسنده ,

  • Issue Information
    روزنامه با شماره پیاپی سال 2010
  • Pages
    8
  • From page
    1094
  • To page
    1101
  • Abstract
    The paper presents a failure case of an aero-engine combustor liner. Macroscopic and microscopic observations, microstructure investigation, chemical analysis and hardness measurement have been performed to investigate the damage mechanism and failure causes of notches and cracks. The results show that the failure modes of notches, axial-direction crack along the combustor liner and crack at the edge of welding spot are respectively attributed to high-temperature ablation, mixed crack of ablation and thermal fatigue crack. The bad configuration of crossover tube is the main reason for the failure of combustor liner.
  • Keywords
    Failure analysis , Combustor liner , Ablation , Thermal fatigue
  • Journal title
    Engineering Failure Analysis
  • Serial Year
    2010
  • Journal title
    Engineering Failure Analysis
  • Record number

    2339005