Title of article
Failure analysis of an aero-engine combustor liner
Author/Authors
Lv، نويسنده , , Fengjun and Li، نويسنده , , Quan and Fu، نويسنده , , Guoru، نويسنده ,
Issue Information
روزنامه با شماره پیاپی سال 2010
Pages
8
From page
1094
To page
1101
Abstract
The paper presents a failure case of an aero-engine combustor liner. Macroscopic and microscopic observations, microstructure investigation, chemical analysis and hardness measurement have been performed to investigate the damage mechanism and failure causes of notches and cracks. The results show that the failure modes of notches, axial-direction crack along the combustor liner and crack at the edge of welding spot are respectively attributed to high-temperature ablation, mixed crack of ablation and thermal fatigue crack. The bad configuration of crossover tube is the main reason for the failure of combustor liner.
Keywords
Failure analysis , Combustor liner , Ablation , Thermal fatigue
Journal title
Engineering Failure Analysis
Serial Year
2010
Journal title
Engineering Failure Analysis
Record number
2339005
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