Title of article :
Failure analysis of titanium alloy (Ti6Al4V) fastener used in aerospace application
Author/Authors :
Jha، نويسنده , , Abhay K. and Singh، نويسنده , , Satish Kumar and Swathi Kiranmayee، نويسنده , , M. and Sreekumar، نويسنده , , K. and Sinha، نويسنده , , P.P.، نويسنده ,
Issue Information :
روزنامه با شماره پیاپی سال 2010
Pages :
9
From page :
1457
To page :
1465
Abstract :
Titanium alloy fasteners are being used in space programme. These fasteners are coated with MoS2, which serves the purpose of solid lubricant. During the trial assembly of flight spin motor to the bracket mounted on subsystem, one of the two fasteners failed such that the head of the bolt had sheared off the shank. Metallographic analysis carried out on the failed fasteners revealed variations in the microstructures all along the shank axis. Microstructure consisted of equiaxed primary alpha in transformed beta matrix within lower portion of the shank, while it was elongated primary alpha with little bulging all along prior beta grain boundaries as well as acicular alpha at some other location towards the head side, features, typical of, as if worked above beta transus temperatures. aper highlights the details of investigations carried out on the failed fasteners.
Keywords :
Bulging of transformed alpha in Ti alloy , Beta transus temperature , Failure of titanium fastener
Journal title :
Engineering Failure Analysis
Serial Year :
2010
Journal title :
Engineering Failure Analysis
Record number :
2339070
Link To Document :
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