DocumentCode :
1184441
Title :
Dynamic Stability Improvvement at Monticello Station-Analytical Study and Field Tests
Author :
Busby, E.L. ; Hurley, J.D. ; Keay, F.W. ; Raczkowski, C.
Author_Institution :
Texas Utilities Services Inc.
Issue :
3
fYear :
1979
fDate :
5/1/1979 12:00:00 AM
Firstpage :
889
Lastpage :
901
Abstract :
Turbine-generator Units #1 and #2 at the Texas Utilities Monticello Station were found to be dynamically unstable when operating near full load and connected to the power system by a single transmission line. Power system stabilizers (PSS) were applied to the excitation systems to provide stable operation under these conditions. Suitable settings for the PSS were predetermined analytically by frequency response and root locus analysis of a single machine-infinite bus configuration. A 3rd order generator model is shown to be adequate for this type of analysis. Dynamic performance measured in field tests is in close agreement with calculated performance.
Keywords :
Power generation; Power system analysis computing; Power system dynamics; Power system modeling; Power system stability; Power transmission lines; Protective relaying; Regulators; Testing; Voltage;
fLanguage :
English
Journal_Title :
Power Apparatus and Systems, IEEE Transactions on
Publisher :
ieee
ISSN :
0018-9510
Type :
jour
DOI :
10.1109/TPAS.1979.319301
Filename :
4113557
Link To Document :
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