DocumentCode :
1456104
Title :
Regulation of a 115-megawatt turbogenerator
Author :
Cornelius, H. A. ; Cawson, W. F. ; Cory, H. W.
Author_Institution :
Public Service Company of Northern Illinois, Chicago, Ill.
Volume :
71
Issue :
3
fYear :
1952
fDate :
3/1/1952 12:00:00 AM
Firstpage :
221
Lastpage :
221
Abstract :
A 115-MEGAWATT 95-per-cent power-factor generator, having a short-circuit ratio of 0.66, has lost synchronism occasionally during faults in the 20 years it has been in service at the Waukegan Station of the Public Service Company of Northern Illinois. During faults the the generator terminal voltage became so low that the generator lost a large share of its load and the rotor accelerated, thus allowing the generator to swing out of synchronism. It was decided to investigate possibilities of using automatic voltage regulation to maintain generator voltage.
Keywords :
Automatic voltage control; Circuit faults; Generators; Regulators; Transient analysis; Turbogenerators;
fLanguage :
English
Journal_Title :
Electrical Engineering
Publisher :
ieee
ISSN :
0095-9197
Type :
jour
DOI :
10.1109/EE.1952.6438003
Filename :
6438003
Link To Document :
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