DocumentCode :
2106626
Title :
Investigation and diagnosis of a 184-MVA air-cooled generator heavily affected by slot partial discharge activity
Author :
Belec, M. ; Li, Sinan ; Nguyen, Duc N. ; Lepine, L. ; Guddemi, C. ; Lessard-Deziel, D. ; Schwartz, Tony ; Lamarre, Laurent
Author_Institution :
IREQ, Inst. de Rech. d´Hydro-Quebec, Varennes, QC
fYear :
2007
fDate :
22-24 Oct. 2007
Firstpage :
85
Lastpage :
90
Abstract :
For many years, partial discharge (PD) activity has been used in air-cooled generators as one of the important indicators of degradation mechanisms in stator winding insulation. Up to a certain level, these degradation processes are slow. Under normal operation, PD measurement and trending can generally indicate that not only electrical but also mechanical, thermal or ambient (contamination) degradation processes are occurring. Partial discharge activity in air-cooled generators also produces ozone so that the presence of ozone inside and around the generator enclosure is indicative of PD activity. In some cases, the ozone concentration produced by sustained PD activity can reach such levels that it becomes a health hazard for plant personnel. Hazardous levels were recorded in 1991, after 12 years of operation, inside the enclosure of the four 184-MVA hydro generators at BC hydro´s peace canyon (PCN) generating station, revealing a situation that was probably active for some years. Results from annual PD measurement performed using PDA (partial discharge analysis) techniques showed an asymmetry in favor of positive discharges that can be the result of slot discharges. Phase resolved partial discharge (PRPD) measurements combined with ozone measurements taken all around the rear perimeter of the generator core were used to confirm the nature of the PDs. Since one of the generators was scheduled for a complete stator winding and core replacement in 2006, an exhaustive investigation was performed before and after replacing the stator. Some stator bars were removed from the slots for visual inspection and extensive laboratory testing. This paper presents results of the on-line PD and ozone measurements, together with findings from visual inspection and laboratory investigations of the retrieved bars. These results were analyzed collectively in order to establish the root cause of the insulation problem as well as the deterioration mechanism of the generator stator wind- - ing. Finally, a new pre-installation testing procedure is recommended to prevent such a costly insulation problem from occurring again.
Keywords :
hydroelectric generators; hydroelectric power stations; machine insulation; machine windings; partial discharge measurement; phase measurement; BC Hydro Peace Canyon generating station; PD measurement; air-cooled generator; ambient degradation processes; apparent power 184 MVA; deterioration mechanism; extensive laboratory testing; generator core; generator stator winding; hydro generators; mechanical degradation processes; ozone measurements; partial discharge analysis techniques; phase resolved partial discharge measurements; positive discharges; preinstallation testing procedure; slot partial discharge activity; stator winding insulation; thermal degradation processes; visual inspection; Inspection; Insulation; Laboratories; Partial discharge measurement; Partial discharges; Phase measurement; Pollution measurement; Stator cores; Stator windings; Thermal degradation;
fLanguage :
English
Publisher :
ieee
Conference_Titel :
Electrical Insulation Conference and Electrical Manufacturing Expo, 2007
Conference_Location :
Nashville, TN
Print_ISBN :
978-1-4244-0446-9
Electronic_ISBN :
978-1-4244-0447-6
Type :
conf
DOI :
10.1109/EEIC.2007.4562594
Filename :
4562594
Link To Document :
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