• DocumentCode
    2387666
  • Title

    Achieving stretched capacity goal through integrated engineering and manufacturing excellence

  • Author

    Kwooi, Reginald See Theam

  • Author_Institution
    Intel Technol., Penang, Malaysia
  • fYear
    2000
  • fDate
    2000
  • Firstpage
    391
  • Lastpage
    394
  • Abstract
    Achieving stretched equipment capacity and high productivity in high volume manufacturing is a gritty challenge to drive down cost continuously in this competitive chipset market. With unprecedented volume ramp of both key products in Q4´99, the Test Module faced a shortage of two to four testers. Driving through working group, a refurbishment process was achieved successfully resulting in 60% reduction of tester faults thus improving mean time between failure (MTBF) from 140 hrs to 160 hrs. With the implementation of improved pogo pins at Tester Interface Unit (TIU) and test head had improved cleaning frequency from 5 k to 90 k, one-sum test yield from 88.7% to 97.5% and reduced non-genuine SBL from 10% to less than 3% consistently
  • Keywords
    integrated circuit manufacture; integrated circuit testing; 140 to 160 hour; Test Module; Tester Interface Unit; competitive chipset market; high productivity; high volume manufacturing; improved cleaning frequency; integrated engineering-manufacturing excellence; mean time between failure; one-sum test yield; refurbishment process; stretched capacity goal; tester faults reduction; volume ramp; Capacitors; Cleaning; Costs; Frequency; Hardware; Magnetic heads; Manufacturing; Power supplies; Productivity; Testing;
  • fLanguage
    English
  • Publisher
    ieee
  • Conference_Titel
    Semiconductor Manufacturing, 2000. Proceedings of ISSM 2000. The Ninth International Symposium on
  • Conference_Location
    Tokyo
  • ISSN
    1523-553X
  • Print_ISBN
    0-7803-7392-8
  • Type

    conf

  • DOI
    10.1109/ISSM.2000.993695
  • Filename
    993695