• Title of article

    Failure analysis of IEU drill pipe wash out

  • Author/Authors

    Shuanlu Lu، نويسنده , , Yaorong Feng، نويسنده , , Faqian Luo، نويسنده , , Terry Changyi Qin and Yuan Pengbin، نويسنده , , Xinhu Wang، نويسنده ,

  • Issue Information
    روزنامه با شماره پیاپی سال 2005
  • Pages
    6
  • From page
    1360
  • To page
    1365
  • Abstract
    Many 127.0×9.19 mm IEU G105 drill pipe failures of wash out occurred after 2367 h of pure drilling time and 8726 m of penetration footage. This paper gives a detailed investigation on these failures and a systematic analysis is carried out on service and loading conditions of the drill pipes. Measurement and inspection were performed on configuration dimensions, chemical composition, mechanical performance, metallography, macro-fractography, micro-fractography, and corrosion products. Configuration stresses at the crack positions of the drill pipe were calculated by FEA. Crack extending velocity of the drill pipe material under corrosion medium was also measured. It is thought from test and analysis results that the drill pipe wash out or fracture accidents were premature corrosion fatigue failure accident. The failure courses were as the following: corrosion pits occurred first on the internal surface at the stress concentrating area of the drill pipe, and then fatigue cracks initiated in pit bottoms, and washed out or fractured subsequently as cracks penetrated through the wall thickness of the drill pipe. The reasons of drill pipe wash out were related to configuration, material quality, and load condition of the drill pipe string.
  • Keywords
    Corrosion pits , Drill pipe , Pickling test
  • Journal title
    INTERNATIONAL JOURNAL OF FATIGUE
  • Serial Year
    2005
  • Journal title
    INTERNATIONAL JOURNAL OF FATIGUE
  • Record number

    1161087